Long time no post, but it shouldn't be too hard to remember everything that happened because it hasn't been much.
I removed and promptly sold the haggard alky system. Sometimes a system is only as good as the installer chooses to make it, but this is one that I've never been impressed with. Most of the vocal turbo Buick guys will disagree with me hard here, but the fit and finish is just terrible. Good riddance.
The installer of my particular unit had no standards. For the system to work right, you need to tap into the MAP sensor and install a new one. He twisted the wires together and wrapped them in electrical tape. That's it. My removal involved removing the wire from the weather pack connecter and shrinking the bare spot. Much better!
In the process I decided to look into the ugly vacuum line situation. I hate that a line was cut for the VDO boost gauge hose. I still haven't figured a permanent solution. In interest of moving on, I pulled the boost gauge hose out of the ugly alky anaconda and otherwise left it as-is. I'll come back to it.
Here's the anaconda I was referring to. I'm so happy to see it go.
I'm not sure if this happened because I was fiddling with it or if was already like this. Either way, it shouldn't have happened. IT does explain why my "Low fuel" light didn't come on when the alky ran dry though. Once again, good riddance!
The only thing I'll miss is he progressive LED which I installed in the A-pillar. It was cool, but I do like less wires.
There's also an LED added in the FACTORY "Power Injection" slot. Word on the street is that Buick intended on selling these cars with a factory methanol injection system, but it got scrapped before production. All that remained was the dummy ligh slot.
Here's another example of poor quality in the kit... instead of adding a bulb holder, a bulb soldered to the wires is just held in with an o-ring. This is original to the kit. It works, but I hate it.
I don't even know what this light was for, but it was attached to the alky system. Oh well. Good bye.
It was so refreshing to see how underwelming the exposed dash looks without the alky rats nest.
Who knew that the plastic kick panel wouldn't sag anymore when you remove a couple pounds from the top of it?! It was such an accepted fate that a support brace was produced. It looks like I won't be needing mine anymore.
More junk that I'm super happy to be rid of.
No more pump.
I got $300 for all that even with extreme transparency about the poor condition. Woohoo!
I had never been so happy to see a yellowed factory coolant reservoir in my life. This moment was pretty monumental for me.
Moving on, I made a move that's very unlike myself. I'm going to remove a very quirky factory option. This car came with a block heater! It's kinda funny, but it's also ugly and unnecessary. The wire is almost impossible to keep free of oil cakes.
Yikes. At least the cord is a standard style that pops right off. The rest of this won't be fun to clean though.
Soon after I had a freak out moment because I saw this very concerning beat up piece of metal in the valley.
After a little bit of measuring and investigation, I realized that it was a turbo bearing! The turbo drains into the valley on these engines. Whew!
After a long delay of waiting for parts and a fancy tool to arrive, I moved on to replacing the valve springs and valve stem seals. Unfortunately, this went very poorly.
I forgot to remove the valve core from my compression tester, and I didn't think setting TDC was necessary, so this happened.
I had no choice but to remove the head.
The only logical thing to do at this point is to remove the rest of the engine. I should have done it from the get go, and it should make the rest of this journey a lot easier. I have yet to figure out how I'm going to get this done with my crappy crane and tiny space in the winter, but I'll figure it out.
Until then, I wanted to make some actual progress instead of tearing more stuff apart.
I thought I was going crazy. You may notice that I "lost" the seal upon spring removal. Installing a new one was not happening for some reason.
I decided to ditch this valve and keep going. That was when I noticed that the exhaust valves didn't have stem seals to begin with! WHAT?! Then I noticed that the valves would never accept a seal even if the guides were machined appropriatley.
https://youtube.com/shorts/7fblKbLdYCk?feature=share
How goofy! No wonder Buicks have an oil burning reputation! I started installing the new Comp dual springs, but I think I'm going to remove them again. I feel like a chump for not cleaning these nasty valves. I might as well!
I also finally finished the blast cabinet, and I couldn't be happier with the results!
I replaced the blue hose with a clear one, because you need to see the media flow while setting the ball valve.
All done featuring a dust deputy between the cabinet and the shop vac.
I can see, there are no cabinet leaks, and the system works great!
I'll let the results speak for themselves. This is before.
And this is after about five minutes with aluminum oxide media.
I can definitely use a water separator and a bigger compressor, but this job was a breeze. I can get away with my 27 gallon for now.