In reply to Floating Doc (Forum Supporter) :
Speaking of other peoples' dumb moments.
Factory Five car. Beautifully done, drove well, sounded weird, didn't seem to have as much power as the Ford Motorsport 302ci crate motor would have suggested. I think you may see where this is going.... the crate motors had roller cams, which all have the 351W firing order. Swapped four plug wires around and it ran EXTREMELY well, and no longer sounded like an aircooled VW.
351C-4V Mustang. Yep, a '71 with the intake ports the size of the ones in a 429.
Didn't seem to run hot by the gauge but it boiled over after you shut the engine off. Hmm. Removed the water pump to find half the bolts were broken off in the block and the heads glued in place, and most of the coolant passages were blocked off by the evil blue silicone. (Do they even sell that stuff anymore?) While the pump was off, decided to check for water flow through the block. No flow from the return passage from the right side head. Someone, somewhere along the way, had put the right side head gasket on backwards, blocking off almost ALL coolant flow through the right side of the engine! It has to go on upside down for the coolant passages to line up. From the looks of it, it had been that way for a LONG time, too!
The head and block were not warped, amazingly. It ran really well after that and a new timing chain (it had the weird -8 factory chain still in it). Also, putting an iron 351C head with iron exhaust manifold attached into a '71 Mustang engine bay suuuuuuucks.
Not to single out Fords. Recieved a '69 Chevelle with a "rebuilt" 350 to finish engine install and sort out. Went to prime the engine. Didn't build much oil pressure and then the drill spun freely. Five quarts of oil on the ground. No oil gallery plugs in the back of the block, all the oil exited stage rear and somehow managed to saturate the clutch disk, too. Removed trans, clutch, flywheel, looked in the holes and could see the cam sprocket at the other end of the galleries - no plugs at that end either. Engine came out after that, and while it was out we stuck a borescope into the plug holes and saw that it had standard size pistons and huge, giant vertical gouges in the bores, and it appeared someone tried to smooth it out by finding some 24 grit stones and honing the bejeezus out of it...